The following day, I got stuck into the reassembly.

To be clear here, these engines were basically a throw-away item, rebuilding one is not an economically viable proposition. So, unless you are sentimental like me and have the time and desire to do so, then you would be better served replacing the engine with a long block for as little as $250. In my case, I used about $70 in parts, a $40 puller, a $60 ring compressor and $20 for ring pliers, so yeah, an extra $60 would have bought me a new engine from an online engine retailer.

Parts for this partial rebuild involved piston rings, and the associated gaskets and seals. I decided to use OEM Briggs & Stratton rings, then aftermarket head and sump gaskets, and a new Stens lower crank seal.

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The first thing I did was to remove the camshaft, lifters and crankshaft cam gear out of the crankcase to provide better access for reassembly. I didn't want to mess with these, but they simply lift out so easily that there was no reason not to. I then cleaned and inspected these parts and set them aside for later. The lifters and (plastic) cam had minimal wear, likewise the conrod and conrod end cap, remarkable considering how much work this engine has done. I then measured old and new rings in the bore to verify that yeah, the old ones were toast.

After giving everything a final clean down, including the cylinder and crankcase, I started by installing the new oil seal on the sump. I then lubed the piston and installed the piston rings, the hardest being the two-piece lower oil control ring which fought me a little. After each ring went on, I staggered the end gaps and clamped it in the ring compressor, which was a little tricky but I got there. Time for everything to go back together!

First up, installing the piston and rod back into the cylinder. After applying oil to the cylinder, the conrod big end and more on the piston, I lined up the piston and ring compressor with the cylinder, then gently tapped the piston down with the handle of my hammer. I don't know if it's just me, but I love the tap-tap-tap sound of a piston being installed into a cylinder. The conrod was then lined up with the crankshaft, both with plenty of assembly oil. I then installed the end cap, again well oiled, then torqued in increments to 11.3 Nm. A quick spin over verified my work.

Next, re-installing the lifters, oiled for good measure. These simply slide back into place, the oiled camshaft then drops into its recess in the block, holding the lifters in place. The oiled crankshaft timing gear slides onto its key, making sure to rotate the crank first to align the timing marks on the gear and camshaft. The camshaft driven oil slinger then drops onto the top of the camshaft.

It was then time to start sealing the engine back up. The gasket kit comes with several paper sump gaskets in differing thickness, I just went with the standard 0.015" item. With the gasket lined up and held with the dowels in the block, I then oiled the crankshaft and oil seal and gently tapped the sump back down till it was nicely seated and flush. I then went around re-installing the sump bolts, firstly winding them down until they seated. Working in a cross pattern, the bolts were torqued down in increments to the 10.17 Nm spec, re-checking a few times to make sure it was all down square.

Next, the cylinder head. Using two of the bolts to hold the new gasket in place, I lined the head up with the block and wound the bolts down until they seated. With the rest of the bolts seated, I then torqued them to 16 Nm, again working in a cross pattern and in increments till the spec was achieved. The supporting bracket was then re-secured and the spark plug installed.

Old worn rings, head gasket and oil seal.

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Getting the engine back on the mower deck took a little patience to align the three bolts with adaptor plate, deck and sump. I then re-installed the blade boss and blade carrier, then connected the throttle cable. While I tend to run 10W-30 semi-synthetic in most of my 4-stroke mowers, but for break-in and on the older Briggs's engines I like to stay with the recommended mineral SAE30. In particular, I've been using Penrite oils over the last few years.

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So, with oil in the sump and fuel in the tank, it was time to fire it up!



Success! yay

Upon first start up, naturally there was some smoke as the engine burnt off the assembly lube. However, as the engine came up to temperature, the smoking cleared, later verified with multiple restarts from hot and cold. Apart from solving the smoking habit, the most noticeable result of this project was how much compression the engine now has, evident from the extra effort required to pull the engine over and how much stronger it sounded.

My biggest fear in the lead up to doing this repair was getting everything back together in the right place. But this engine is so bloody simple, that when I stepped back and thought about it yesterday, it's almost impossible to put it back together the wrong way. The piston and rod assembly can only go one way, otherwise you wouldn't have access to the end cap bolts. The camshaft, lifters and timing gear are all recess fit, making it simple to remove and re-install correctly.

[Linked Image from i.postimg.cc]

[Linked Image from i.postimg.cc]

As I said earlier, you would never rebuild one of these engines unless its something you really wanted to do, simply because of the throwaway society we live in. And a small engine shop wouldn't want to do it either, the argument being that parts and labor to do so would probably buy you two brand new engines!

But that was not the point here. I wanted to do this for sentimental reasons, but also out of curiosity. As a bonus, I got to learn how to use a puller and piston ring compressor, while also putting my tools to good use. As a learning experience, I would call it a success. But to have also achieved the desired result, as in no more smoking, well that makes me very happy.

(Sorry about the lack of photos for this project. I was covered in oil and filth, which I didn't want all over my camera or phone, and I was also focused on the task at hand.)